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Density Test Report
Concrete Test Report
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Daily Field Report
Density test report
Date
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Project Number
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2024C168(Reserve @ Gum Springs)
Name of the Project
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Project Location
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Client Company
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Weather
Arrival Date
Arrival Time
Departure Date
Departure Time
Onsite Hours
ASEC Technician Name
amin.azimi@asec-na.com (Aminullah Azimi)
Observations/Finding
Summary
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<span style="font-family: arial, helvetica, sans-serif">As requested, the site was visited by our AS Engineering and Consulting (ASEC) representative for the purpose of providing quality control inspection and testing services. Visual observation techniques were employed to verify compliance with project drawing/specifications, </span><span style="font-family: arial, helvetica, sans-serif">applicable codes, and materials submittals. The following observations were observed on site this day.</span> <ul> <li><span style="font-family: arial, helvetica, sans-serif">A proof-roll observation and density tests were performed on the road (locations are shown in the pictures) and work was on progress at water line in the front from lot# 115 to lo#118 and lot#150 and also in the front of lot#113 to lot#222 and also work was on progress on lot#1, lot#2, Lot#3, Lot#4, </span><span style="font-family: arial, helvetica, sans-serif">on this day.</span></li> <li><span style="font-family: arial, helvetica, sans-serif">At the time of arrival, our representative observed that the backfill lift was being placing 1 foot using a 20-ton pad-foot Compactor. Compaction testing was performed using a Troxler nuclear density gauge (ASTM D 6936), along with general probing using a 3/8" diameter probe rod.</span></li> <li><span style="font-family: arial, helvetica, sans-serif">Density test results indicate that most of the compacted materials met the project requirement of 95% of the maximum dry density obtained by a Standard Proctor ASTM 698, </span></li> <li>A proof-roll observation was performed on the Road (location shown in the picture).</li> <li>A fully loaded tandem-axle dump truck was used to proof-roll the above-mentioned subgrade with multiple passes across the area.</li> <li>Some yielding and deflection were observed during the proof-roll at all areas mentioned below. (Locations are shown in the pictures)</li> <li>Size (25'x5') (118'x19') (50'x9') (45'x7') (31'4') (73'x7') (40'x19') (18'x5') (19'x5') (45'x5') (15'x5') (13'x5')</li> <li>Contractor was informed and it was recommended to undercut approximately 6 inches of soft soils in select areas and replace with compacted GAB.</li> <li>Our representative along with Belly of Allied Pavement and the Neal Foster Bureau Ventas North America Inc, representative and Derak with Century observed the proof-roll.</li> </ul> We appreciate the opportunity to be of service to you on this project. If you have any questions regarding this report, please feel free to contact us. We will be more than happy to discuss it with you.
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