Skip to content
Menu
Home
About
Daily Field Report
Density Test Report
Concrete Test Report
Login
Home
About
Daily Field Report
Density Test Report
Concrete Test Report
Home
Daily Field Report
Density test report
Date
*
Project Number
*
2024C168(Reserve @ Gum Springs)
Name of the Project
*
Project Location
*
Client Company
*
Weather
Arrival Date
Arrival Time
Departure Date
Departure Time
Onsite Hours
ASEC Technician Name
amin.azimi@asec-na.com (Aminullah Azimi)
Observations/Finding
Summary
*
<span style="font-family: arial, helvetica, sans-serif">As requested, the site was visited by our AS Engineering and Consulting (ASEC) representative for the purpose of providing quality control inspection and testing services. Visual observation techniques were employed to verify compliance with project drawing/specifications, </span><span style="font-family: arial, helvetica, sans-serif">applicable codes, and materials submittals. The following observations were observed on site this day.</span> <ul> <li><span style="font-family: arial, helvetica, sans-serif">The placement and compaction of fill for Lots #131, 132, 133, 145, 146, 147, 171, 170, 169, 168 and the sewer trench between MH A10 to C1 and the storm water trench between MH C2 to MH C3 and storm line between A2 to A3, continued this day.</span></li> <li><span style="font-family: arial, helvetica, sans-serif">At the time of arrival, our representative observed that work was in progress with 1-foot lifts being placed and compacted using 815F and CP56B compaction equipment. Compaction testing was performed using a Troxler nuclear density gauge, along with general probing using a 3/8" diameter probe rod.</span></li> <li><span style="font-family: arial, helvetica, sans-serif">Density test results indicate that the compacted materials met the project requirement of 95% of a maximum dry density obtained by a Standard Proctor ASTM 698. </span></li> <li><span style="font-family: arial, helvetica, sans-serif">Note: one test for backfill at the sewer trench between MH A10 and C1, did not meet the project requirement of 95%. Contractor was informed to aerate and recompact.</span></li> </ul> We appreciate the opportunity to be of service to you on this project. If you have any questions regarding this report, please feel free to contact us. We will be more than happy to discuss it with you.
Upload Images
Image
Description
1
2
3
4
5
6
7
8
9
10
11
12
13
1
Add Row
Post Status custom
Validate Email
Visual
Text
Insert/edit link
Close
Enter the destination URL
URL
Link Text
Open link in a new tab
Or link to existing content
Search
No search term specified. Showing recent items.
Search or use up and down arrow keys to select an item.
Cancel