Skip to content
Menu
Home
About
Daily Field Report
Density Test Report
Concrete Test Report
Login
Home
About
Daily Field Report
Density Test Report
Concrete Test Report
Home
Daily Field Report
Density test report
Date
*
Project Number
*
2024C112(Sterlington)
Name of the Project
*
Project Location
*
Client Company
*
Weather
Arrival Date
Arrival Time
Departure Date
Departure Time
Onsite Hours
ASEC Technician Name
amin.azimi@asec-na.com (Aminullah Azimi)
Observations/Finding
Summary
*
At the request of the client’s representative, our AS ENGINEERING AND CONSULTING, LLC (ASEC) representative visited the job site to visually observe the contractor's work activities from a quality standpoint to verify compliance with project drawings/specifications, applicable codes, and materials submittals and conducted QC testing per the project drawings and specifications. The following observations were made on site this shift: <ul> <li><span style="font-family: arial, helvetica, sans-serif">A proof-roll observation was performed on the road (the curbline).</span></li> <li><span style="font-family: arial, helvetica, sans-serif">A fully loaded tandem-axle dump truck was used to proof-roll the above-mentioned subgrade with multiple passes.</span></li> <li><span style="font-family: arial, helvetica, sans-serif">No severe yielding and/or deflection was observed during the proof-roll at all areas mentioned above.</span></li> <li><span style="font-family: arial, helvetica, sans-serif">The placement and compaction of backfill for Lot #19 and Lot #12 continued this day.</span></li> <li><span style="font-family: arial, helvetica, sans-serif">At the time of arrival, our representative observed that work was in progress with 1-foot lifts being placed and compacted using a 15-ton sheeps-foot CP54B compactor. Compaction testing was performed using a Troxler nuclear density gauge, along with general probing using a 3/8" diameter probe rod.</span></li> <li><span style="font-family: arial, helvetica, sans-serif">Density test results indicate that the compacted materials generally did not meet the project requirement of 95% of the maximum dry density obtained a Standard Proctor ASTM 698. </span></li> <li><span style="font-family: arial, helvetica, sans-serif">We appreciate the opportunity to be of service to you on this project. If you have any questions regarding this report, please feel free to contact us. We will be more than happy to discuss it with you.</span></li> </ul>
Upload Images
Image
Description
1
2
3
4
5
6
1
Add Row
Post Status custom
Validate Email
Visual
Text
Insert/edit link
Close
Enter the destination URL
URL
Link Text
Open link in a new tab
Or link to existing content
Search
No search term specified. Showing recent items.
Search or use up and down arrow keys to select an item.
Cancel