Skip to content
Menu
Home
About
Daily Field Report
Density Test Report
Concrete Test Report
Login
Home
About
Daily Field Report
Density Test Report
Concrete Test Report
Home
Daily Field Report
Density test report
Date
*
Project Number
*
2023C180(Lakeside Sub. - Lovers Lane, Calhoun)
Name of the Project
*
Project Location
*
Client Company
*
Weather
Arrival Date
Arrival Time
Departure Date
Departure Time
Onsite Hours
ASEC Technician Name
russell.hendrix@asec-na.com (Russell Hendrix)
Observations/Finding
Summary
*
As requested, the site was visited by our AS Engineering and Consulting (ASEC) representative for the purpose of providing quality control inspection and testing services. Visual observation techniques were employed to verify compliance with project drawing/specifications, applicable codes, and materials submittals. The following observations were observed on site this day. <strong>Location:</strong> Section from 4.4 to 4.5 <strong>Summary:</strong> Continuation of the placement of sanitation sewer from 4.4 to 4.5 was undertaken on this day. An 8-inch ductile iron pipe was utilized on the main line. Rock was encountered just south of 4.5, necessitating the use of a hoe-hammer for one hour. recommendations made for compaction methods and lift depths were not followed. Testing was hindered due to the depth of the trench. Excavation for the next lateral northeast of 4.4 (087-02) was initiated. <strong>Key Events:</strong> <ol> <li><strong>Main Line Placement:</strong> <ul> <li>An 8-inch ductile iron pipe was used for the main line sewer from 4.4 to 4.5.</li> <li>Rock was encountered just south of 4.5, requiring the use of a hoe-hammer for excavation.</li> </ul> </li> <li><strong>Bedding Materials:</strong> <ul> <li>For the lateral northeast of 4.4 (086-02), 6 inches of 57 stone was utilized for bedding, while graded aggregate base (GAB) was used for the remainder beneath the future road.</li> <li>Lift depths varied, with approximately 2 to 3-foot depths for the lateral and 4 to 5-foot lifts for the main line between 4.4 and 4.5.</li> </ul> </li> <li><strong>Compaction Recommendations:</strong> <ul> <li>Trench packer and riding vibratory sheepsfoot were employed for compaction.</li> <li>A recommendation of 6-inch lifts for compaction using the trench packer and 12 inches with a ride-on vibratory roller was provided to the foreman but not followed.</li> </ul> </li> <li><strong>Testing Constraints:</strong> <ul> <li>Testing could not be completed due to the depth of the trench, which impeded access for testing equipment.</li> </ul> </li> <li><strong>Excavation of Next Lateral:</strong> <ul> <li>Excavation for the next lateral northeast of 4.4 (087-02) commenced.</li> </ul> </li> </ol>
Upload Images
Image
Description
1
sanitation sewer facing 4.4
2
compacting sanitation sewer at 4.4
3
4.4
4
4.4 with Lateral (GAB)
5
4.5 location (not set)
1
Add Row
Post Status custom
Validate Email
Visual
Text
Insert/edit link
Close
Enter the destination URL
URL
Link Text
Open link in a new tab
Or link to existing content
Search
No search term specified. Showing recent items.
Search or use up and down arrow keys to select an item.
Cancel