Skip to content
Menu
Home
About
Daily Field Report
Density Test Report
Concrete Test Report
Login
Home
About
Daily Field Report
Density Test Report
Concrete Test Report
Home
Daily Field Report
Density test report
Date
*
Project Number
*
2022C207 (draft)(CME Church Education Center)
Name of the Project
*
Project Location
*
Client Company
*
Weather
Arrival Date
Arrival Time
Departure Date
Departure Time
Onsite Hours
ASEC Technician Name
Isaac Davis (Isaac Davis)
Observations/Finding
Summary
*
<strong>Report on Jobsite Assessment at UMC Church</strong> <em>Project Overview:</em> The assessment at the UMC Church jobsite involved conducting tests on various sections designated as A/2, C/2, D/2, G/2, K/2, L/2, and the retaining wall for the mechanical room. The specified bearing requirement is 1500 PSF. The footings were filled with #57 stone, followed by approximately 2 to 3 feet of gravel, layered atop the old existing parking lot surface. <em>Section Analysis:</em> <ul> <li><strong>A/2</strong>: Excavated to around 1 foot deep; initial DCP testing resulted in a blow count of 12. Further hand augering reached approximately 1 foot 5 inches, followed by Auger Refusal (AR) with the DCP.</li> <li><strong>C/2, D/2, G/2</strong>: All sections were hand augered to around 2 feet 6 inches. At 1 foot depth, C/2 received 8 blows, D/2 got 10 blows, and G/2 received 11 blows.</li> <li><strong>K/2 and L/2</strong>: Both end sections received blow counts of 9 blows.</li> <li><strong>Retaining Wall for Mechanical Room</strong>: With a 2-foot height, the excavation reached 1 foot deep. The first foot resulted in a blow count of 12, while the subsequent foot received 9 blows.</li> </ul> <em>Observations and Compliance:</em> All measurements and tests conducted align within the specified parameters. The excavated sections are scheduled to be replaced with #57 stone as per the specifications outlined. <em>Conclusion:</em> The assessment indicates that the conducted tests and excavations are in accordance with the specified standards and requirements outlined in the plans for soil bearing pressures. The replacements with #57 stone in the dug-out sections appear to be in line with project guidelines.
Upload Images
Image
Description
1
2
3
4
5
6
7
1
Add Row
Post Status custom
Validate Email
Visual
Text
Insert/edit link
Close
Enter the destination URL
URL
Link Text
Open link in a new tab
Or link to existing content
Search
No search term specified. Showing recent items.
Search or use up and down arrow keys to select an item.
Cancel